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20th August 2012
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XL FORUM TEAM MEMBER
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Join Date: Apr 2012
Posts: 334 Sportster/Buell Model: Sportster 1000 Sportster/Buell Year: 81
Reputation: 164
 
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Kiehin buttetfly tune
Ok, i have been changing jets and stuff 2 weeks now and cant get it right. I now have 170 main and 88 pilot. If i turn mixure out it starts to stumble around 2 1/2 turns . I turn it in and can go all the way to seated and just gets a little rough . I set it about 3/4 seemed ok but after ride it wouldnt idle at all. Also noticed rear cylinder exhaust is real sloppy sputtering. Also popping thru exhaust when i let off throttle. I have adjusted rods and rechechecked. Sprayed intake no sign of leaks. Carb is clean as new. I am lost . I have jetted many bikes before but this one just is not working out... Thanks
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20th August 2012
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Know It All
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Join Date: Jun 2012
Posts: 178 Sportster/Buell Model: XLH Sportster/Buell Year: 1977
Reputation: 51

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Do you know if you are running rich or lean? What do your plugs look like? I've finally got mine dialed in and it stalls at 1/4 turn out going in so you pilot jet may be to big for starters.
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I'm just a newb with an ironhead, a toolbox, a computer and a FSM.
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20th August 2012
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XL FORUM TEAM MEMBER
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Join Date: Dec 2009
Posts: 525 Sportster/Buell Model: xlch Sportster/Buell Year: 1973
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I had a similar problem after many attempts at changing jets doing timming and push rods .It would run good then after a short ride it would play up again allways fouling the front plug .For the life of me i could not work out why .Then i done a leak down test and found front inlet valve leaking .Pulled the front head and the valve seat insert was cracked.Going by your previous posts you have gone up and down the jet scale. Try doing a leakdown test it dont cost nothin and it will rule out valve and ring problems .
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hell on two wheels
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20th August 2012
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XL FORUM TEAM MEMBER
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Join Date: Apr 2012
Posts: 334 Sportster/Buell Model: Sportster 1000 Sportster/Buell Year: 81
Reputation: 164
 
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Its running rich... Plugs are black
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20th August 2012
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Rider Of The Iron Steed
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Join Date: Dec 2003
Location: London, ON Canada
Posts: 23,708 Sportster/Buell Model: XLH Sportster/Buell Year: 1978
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+1 on doing a thorough check for intake and exhaust leaks. It is impossible to tune up the carb if these are not completely sealed up.
Set the pilot screw when the engine is fully warmed up, as in a half hour ride not in the city, then leave it there. If there is a probem it is not because of the pilot screw setting.
In my experience plugs will always be black after a ride in the city. It has to be out on the hiways. I use the local paved roads with little traffic.
Tuning a carb in the shop is problematic. Best done out on the back roads.
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20th August 2012
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Senior Chief Know It All
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Join Date: Mar 2011
Location: State Side
Posts: 810 Sportster/Buell Model: XLCH Sportster/Buell Year: 1974 Other Motorcycle Model: 1999 FLHTCUI
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88 pilot is way too big, particularly since you can turn the mixture adjustment screw that far out, and all the way in and it makes almost no difference in how it idles.
Like already said, you must verify all the little things before you try to fine tune the motor. Make sure valves are adjusted properly, timing is set where it should be, advance mechanism is working (if you have it), and most importantly, there are no intake or exhaust leaks. If one of these things is off, you will never get it to run right.
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20th August 2012
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Rider Of The Iron Steed
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Join Date: Dec 2003
Location: London, ON Canada
Posts: 23,708 Sportster/Buell Model: XLH Sportster/Buell Year: 1978
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Quote:
Originally Posted by ultra...good
... Like already said, you must verify all the little things before you try to fine tune the motor. Make sure valves are adjusted properly, timing is set where it should be, advance mechanism is working (if you have it), and most importantly, there are no intake or exhaust leaks. If one of these things is off, you will never get it to run right.
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+1
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21st August 2012
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Senior Master Custom Bike Builder
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Join Date: Dec 2007
Location: Australia
Posts: 7,851 Sportster/Buell Model: XLCH 1000 Sportster/Buell Year: 1977 Sportster/Buell Model #2: 75 motor in Norton frame. Other Motorcycle Model: 42WLA 45, Harton, Narley Other Motorcycle Year: 1942
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If you are running the 34mm Keihin, which is stock your year, the 88 slow jet is most likely too big, which is why you can close the idle mix screw all the way down and it still runs ok. Too much fuel going in via the slow jet at idle.
I run an 88 in my 38mm Keihin so suspect its too big for your 34mm.
Or your float level is set too high and is slopping extra fuel into the carb at idle.
Or you accelerator pump is dribbling fuel through into the carb at idle. Might need the pushrod on the pump shortening so it does not prop the diaphragm open at idle, or might just need cleaning out.l
__________________
In theory there is no difference between theory and practice. In practice there is.
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21st August 2012
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Rider Of The Iron Steed
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Join Date: Dec 2003
Location: London, ON Canada
Posts: 23,708 Sportster/Buell Model: XLH Sportster/Buell Year: 1978
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Quote:
Originally Posted by hopper
if you are running the 34mm keihin, which is stock your year, the 88 slow jet is most likely too big, which is why you can close the idle mix screw all the way down and it still runs ok. Too much fuel going in via the slow jet at idle.
I run an 88 in my 38mm keihin so suspect its too big for your 34mm.
Or your float level is set too high and is slopping extra fuel into the carb at idle.
Or you accelerator pump is dribbling fuel through into the carb at idle. Might need the pushrod on the pump shortening so it does not prop the diaphragm open at idle, or might just need cleaning out.l
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+1
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21st August 2012
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XL FORUM TEAM MEMBER
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Join Date: Apr 2012
Posts: 334 Sportster/Buell Model: Sportster 1000 Sportster/Buell Year: 81
Reputation: 164
 
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Ok tonight i checked intake again no leaks. Went ahead and replaced clamps and seals i had new ones sitting here. Went ahead and took it down to a 80 pilot jet and think i got it.will no for sure tommorow after work.
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